Saturday, December 12, 2009

Over to Granville Island for the finishing touches


A new hatch for the aft deck.

The original teak hatch had become very weak after it was sanded by the company that painted the decks, they had sanded through the screw ends which were holding the wood to the bronze ring. They painted the hatch the same as the decks to hide the problem.

When it was stripped of the paint and reassembled there wasn't much wood left, the screw holes were plugged and new holes drilled. The wood was weakened and delaminated once it was put back in service.

A stainless ring was ordered and polished to a mirror finish, 1/2" plexiglass was cut, laminated to a 1/4" of frosted plexi and reassembled keeping the original chromed ring for detail. The wood ring with the chocks remains on the underside, protected from our wet weather.




These are the Holley carbs that were rebuilt in Southern California by a connection of Jimmy the engine specialist who helped rescue the summer.


The engine bolts are being picked out in silver along with the dip stick and filler caps.


Sunday, August 23, 2009

Old School "Made in the USA" Ford 427

The Crew Cruise was not without failure. The starboard engine stalled and refused to start again. Captain Doug brought her back to the dock on one again. Enough said.

Dr D was on the scene the next morning diagnosing an over heating coil. It was a new coil and research is continuing after replacement. Mallory old school tach drive distributors with new electronic ignition, new coil with internal ballast or should we be back to old school external resistor with points?

The question has been posted to Mallory to get new original distributors or have these factory rebuilt.

These engines ran fine for 40 years with points, sure the points are a little more maintenance, the set-up for the ceramic ballast seemed beautifully engineered. Have we adopted new technology needlessly?

Below are two videos featuring the 427 engine - as Paul in the boat yard said when he heard of the failure - "That's what you get with hot-rods."

The engines are the finest hour for American automotive design. Having a pair in a beautiful Chris Craft from the same period of prosperity in North America has to make you stop and wonder how we ever lost the edge and became consumers of foreign made cheap imitations.









Thursday, August 20, 2009

The Crew Cruise - a salute to those still standing

At the end of the long, expensive (as in - beyond your worse nightmare expensive) and at times very trying (to put it politely) restoration of Paramount, Doug and Mrs T invited those not directly responsible for the torture for a "Crew Cruise".


Mrs T - Mrs Terrible - Doug's nick name for his bride of 20 years, Nicole - pictured here with Rockin' Robbie's gal Cindy on the left.


Dr Doug, resplendent in his polyester sky blue shirt matching the Vancouver evenings sky to perfection, was the principle architect and the critical eye. Doug only does what Doug does well. A one-man-band in a very quiet way. His experience and knowledge base are second to none.

Below are a couple of comments posted on the Chris Craft Commander Forum by fellow Commander owners:

That is just AWESOME May 26 2009

That is without a doubt the finest 47 I've ever seen, and there are a lot of very nice ones. Really sorry the engine setback had to happen, but, well.... been there. Sounds like you're in good hands though.

Eric

Very excellent job on everything including the detail down to the red safety tips on the hose clamps. Beautiful boat and workmanship on everything. Motor issues aside, you should be good and ready for summer Pac Northwest style as we say here in the lower 48. I don't think I ever saw any better wiring job under the hood of a BMW.

JB



Paramount is off the dock with her incredible Ford Cobra engines thanks to one man. Jimmy Richmond.

Jimmy (left) and his race ready assistant Aaron (missing for a wedding rehearsal) dyno tested the rebuilt, rebuild engines. After the first over-compressed pair of 427's melted down 20 minutes into Miss P's first sea trial, Jimmy was brought in to oversee the rebuilding and dyno testing of the replacement engines.

Jimmy tested and rejected the starboard engine twice before it was cleared on the third run. Problems identified in the starboard engine were double checked on the port engine, any similar problems were corrected before the port was given room on the bench.

Without his expertise, we would have been back at square one (stuck on the dock) for the second time. He picked up incorrect sized valve springs, reverted the side oiler back to a side oiler after the shop "modified" it and found a leak in the exhaust manifold that was letting water into the block.

That's Robert from Granville Island Boat Yard in the grey shirt with the red band. Rob with his "can do" attitude stayed late to help lift Paramount for the engines to go back in. Rob is a true boater, always smiling when shit happens - "that's boats for you", he knows patience will be rewarded.


Gord (right) - the man with the long reach - he changed his schedule dozens of times to accommodate the engines being returned and lifted back into the boat. The man that makes a very difficult operation go smooth as silk. Gord's dexterity with his crane boom is surreal.

He's chatting to Andrew, the Lambert's houseman, seconded to the boat to help with the installing and trimming of the headliner and a multitude of other finishing touches to complete the interior.


Left to Right

Sue, girlfriend of Robert (GIBY) a nurse and go with the flow gal. She's always smiling and knows Rob is a perfectionist around the boat yard. He doesn't rush and Sue is always happy to help or get out of his way. He's like a kid in a toy store.

Captain Scotty - wearing the Pirates T-shirt. That's a hint. Scotty scrubbed and scoured the bilges for weeks. He erased 40 years of wear and tear preparing the engine room for the return of the "big dogs". Scotty jumped to do whatever was asked. The swim grid sanded and oiled to a fine finish, the decks routinely cleaned during the restoration, every screw in the trim along the hull he removed and replaced, fresh sealant added for a water-tight Miss P.

Rockin' Robbie and his gal Cindy. Rob scraped, sanded, and faired the bottom of Miss P. Taking off the years of paint to the fresh bottom factory gel. He painted the coats of epoxy protectant to a smooth perfection, adding two coats of anti-fouling to her for the season ahead.

Mrs Terrible, terrible in the best way. She always loved the boat, but the smell of emulsified oil in the bilges, permeating the cabin combined with the dampness and mold spores in the headliner were just too much for her to really enjoy being onboard.

Nicole rolled up the sleeves of Doug's coveralls and hi-ho it was off to work she'd go. In with Scotty scraping and sanding the bilges, pulling out the fridge, getting into every nook and cranny. Out with the old and smelly, in with the new and extremely tasty.

Down came the headliner that was heading that way on it's own, off came the wall paper that was so ready to go. Every detail scrutinized and refined, the new gold flecked curtains, faux lizard skin wall paper and the leopard carpet breathing new life into their ship of dreams.

Nicole and her designer friend Liz nominated Norm pictured below in the "wive's club" for his skill in getting Doug to keep opening his wallet and paying for more. It was fine for Doug to escape to his Paramount, but dear Nicole just though old old old. For the safety of the family and the sense of her nose she knew the money had to go.

Norm did what he could, taking to heart Doug's words; Treat her as if she were your own.

Saturday, August 8, 2009

The first week aboard the "New Paramount"

Left Vancouver Harbour 0700 hrs arrived RVYC Scott Point at 1300 hrs - transiting through Gabriola Passage into the nice calm waters of Trincomali channel .


Departed Scott Point Aug 6 at 1700hrs through Navy Channel and Plomper Sound arriving Lyall Harbour Saturna island at 1800 hrs.


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Had a great dinner and overnight ashore with our friends Al and Lianne Peretz, and departed the next day Aug 7 at 1200hrs , but not before draining the local fuel dock dry of gasoline ( at $1.38 @ L !!! ) - for our journey home through Trincomali Channel, Poirier Pass ( with a 6 knot flow speeding us along ) - arriving False Creek Yacht Club, 1730 hrs with a 10 knot winds and following seas.


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With the weather getting much cooler we were all ready to get back to the house after a wonderfull first week aboard the new Paramount !

Estimate fuel consumption closer to 50 percent better ...
rodl (rolling on dock laughing) over zach and the pee still ....

Pictures to come...

Sunday, August 2, 2009

Paramount's first trip with the Precious cargo


Saturday 1st August 2009


Miss P leaves the dock at 14:00 hours with Mrs T, Ali, Gab and Zach onboard for the long awaited summer holiday cruise to the Gulf Islands. Arriving at 0000.

Engine Hours:

Flawless cruise to salt spring - amazing !!!
Except for zach getting stung by man-o-war and our whole crew having to pee on him .....too funny ....


2800 rpm - was good speed ...

10 knots with whaler in tow - fuel consumption wayyyyyy down - at least 30 percent better ....

Tides:
09:29 1.1 3.6
17:22 4.2 13.8


Salt Spring Island


One of the most beautiful islands in the Southern Gulf. The Saturday Market is an amazing collection of local organic growers, bakers, cheese makers and other towns folks who sell handmade furniture, and other artistic wears. The colours and displays are beautiful. The quality and the taste - gourmet by any standards. It is a place that reminds us of simpler times, when the market wasn't global.


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Saturday, August 1, 2009

Engines Rebuilt (again)

So far - so good.

What went wrong with the first pair;

11-1 compression Keith Black Hypereutectic Pistons, a side-oiler "converted" to a top oiler, shabby rebuilt Holley carburetors, shabby rebuilt distributors, wrong sized valve springs. What am I forgetting?

The pistons were shipped as part of a "Deluxe Rebuild Kit" from Performance Suspension Technology. They sent pistons that would be right for a hot-rod racing machine, but totally wrong for a marine installation. It wasn't picked up by the machinist.

The carbs and distributors went out to local shops for rebuilds. The carbs looked like they hadn't be touched. The distributors couldn't have been.

For round two, the pistons were changed to forged KB dished with a compression rating of 9.1-1, a thicker gasket was used for the heads reducing compression further. The carbs went to a shop in Southern California and came back looking like they were new out of the box. The distributors have been sent to another So-Cal outfit and a spare pair are being used in the short term.

The proper bearings and cam were flown in for the side-oiler. Which was purchased for parts and rebuilt first as the machine shop waited for the engines out of the boat. The engines in Paramount were top-oilers and this was also missed until the spare engine was rebuilt. When they started on the other engine they realized there were two different engine builds.



Jimmy Richmond, Richmond Engines and his right-hand Aaron were responsible for the dyno testing this round. There help was invaluable. They found the springs to be incorrect on the valves. They picked up condensation "like H2O" said Aaron in the oil filter after running the engine they cut the filter in half to check it. Thorough to say the least!

By the time they signed off one engine had to be dyno tested three times, whilst the other was run twice. Their diligent efforts saved us from another catastrophe.


Here is some film looking over the transom at the wake and exhaust of Paramount.

Saturday, July 18, 2009

Canadian Pacific Flagship

Paramount has been bestowed the title of Canadian Pacific Flagship

It is a great honor to be recognized as one of the finest Chris Craft Commanders in the world, by The Chris Craft Commander Forum, Inc.

Paul the forum founder has been an incredible help getting Paramount back together again.





Friday, April 24, 2009

Back to the Island

Catastrophic Engine Failure!

After a short tow from Paramount's berth around to Granville Island, the boys get her ready for the engines to go back to the shop for forensic analysis to determine where the failure occurred. 

Was it just the wrong sized pistons with their 11-1 compression ratio? Or was it something else that started the heat that started the meltdown?

The Granville Island Boat Yard guys stayed back after hours to do a quick lift. A two hour quick lift! The engines were out in a flash - Gord the crane wizard, and all the crew were keen to catch the Canucks playoff game.



Tuesday, April 21, 2009

Comment From Paul, Founder of The Chris Craft Commander Forum


The Internet is a small world...


Paul has commented on this blog site - he must have found it on his own. We had been waiting to write to his website after everything was finished on Miss P. 

He has beat us to it, and comments on our engine problems. He is THE MAN - when it comes to Chris Craft Commanders, he is the founder of the CCC Forum, an architect by trade, a Chris fanatic by admission. We are grateful for his website and value his comments on our situation immensely. This is what he has written:

"Man I am soooo sad to hear news like this, especially after you have put your heart and soul into the restoration. I note the use of Keith Black pistons, many people have used these as a basis for custom 427 pistons with good results.


The only things I can imagine that would cause the motor to heat up like that would be poor ignition/fuel mix, a very poor automotive timing setting (and not following the dimple on the flywheel at 500-RPM while in gear for the marine Chris Craft setting), or a leaned out fuel mix (or both simultaneously), or perhaps an impeller that went out causing a catastrophic over-heating of the motor while running at speed. 

Forensic review of the impeller and strainer, and coolant would give an indication of their integrity. 

This could have been caused by advanced ignition timing, wrong plugs, lean fuel, intake manifold vacuum leak, sticking valves (perhaps incorrectly set for a solid lifter motor), insufficient cooling, poor lubrication. 

I have considerable resources I can share with you if you need them on the 427 marine motor. Drop me a line at ChrisCraftCommander@hotmail.com
and I'll do whatever I can to assist.

Sincerely,

Paul

Thursday, April 16, 2009

Melt Down!


The Keith Black Pistons Blow Apart

The engine has been stripped down in the boat. The damage is extensive - all eight pistons have blown apart or are on their way. The aluminum got so hot it vaporized - large pieces of the pistons are missing.





We are investigating the cause. The timing was checked twice. The carb was rebuilt. They performed perfectly in the dyno test.

Oil samples from the other engine are being analyzed and we should know this morning if the port engine has done the same thing. With all eight affected in the starboard the port will need to come out as well. 







It was a very sad day for everyone involved in the restoration - she was running beautifully before the meld down. She was clipping along at 19 knots. 


Dr Doug has jumped in to help rescue the disaster. He's been in the bilges helping G get to the bottom of the engine and wasting no time to resolve this for Captain Doug who is pictured here running the good doctor, with his wheel barrel and tools, back to Granville Island.

It was time to cry in the beer.

Sunday, April 12, 2009

"I still don't want bowling shoes ..."

Despite the most major of set-backs on the first sea trial for Paramount - Captain Doug isn't willing to trade in the deck shoes.

After months of labour & tons of TLC everything is restored to as new - all systems have been upgraded, the engines bench tested - Miss P is a looking and feeling like a new boat and she's ready to go for a first burn.

  

Everything was going beautifully for the first 1/2 hour at RPMS below 3000. Paramount was up and out of the hole at 2800 making 9 knots in a 4 knot tide on the bow. On a slack or slower tide she should be out of the hole sooner and a knot or two quicker.


Below is the view from the bow at around 3000 RPM running around 14 knots, into the tide. Paramount is up and sitting pretty. She's hasn't run this well for Doug, she's feeling sporty at the wheel, a slight correction and she is on her new heading with no delay.






A fine moment - the Captain at the wheel, feeling the difference in power and response. His beautiful boat is running like new.

Friday, March 27, 2009

A Pair of Kittens


After so many hours spent researching, emailing, tracking down parts, cleaning, prepping and rebuilding at considerable expense, the two original 427 engines are truly better than new







They are back in Paramount and ready for the final helm wiring to be run. They were dyno tested at 340 HP and with the original exhaust manifolds and cooling system they should be good for 30-40 HP more.


It is Friday night and Dr Doug has had a long week. As he searches his pockets looking for his trusty Swis Army knife which he has forgotten he has used in place of the machinists standard clothes peg to keep the choke open. Can he find it? Of course he can! At the end of the video Doug's hand gesture says it all...finished, a job well done!


Thursday, March 26, 2009

Getting there - one day at a time...


The months have flown by since her restoration project started. Dr Doug has been holed up in Paramount for the past two months working on the last major upgrade to be done - the wiring. 

The new and very subtle "lizard skin" wallpaper is up, the headliner looks beautiful, the brightwork is looking bright and the million pieces of the puzzle are now returned to their correct place. The mast is standing and the chrome looks stunning.

 A red night light has been added to the helm, great underway and a nice touch at the dock entertaining.

.

Dr Doug has rewired the old gal, the engine room now glows with 12V lights, no need for trouble lights now! The house bank of 6 gel batteries will keep the music playing all night long.


The area that was used for the main panel is now used as the relay area bringing the vast number of wires into one neat and accessible junction - with the new panel moved over to the small cupboard. All of the electronics are routed to the one place, stereo, battery switches and breaker panel.


Bring on the roar, or is that a purr?


The engines are ready to go! Here Doug tightens up the sea strainer. A new nylon washer will stop the drip. We are opening the sea cocks to start the engines in the boat for the first time.




Saturday, January 31, 2009

Closer to Splash!


The dust has settled and Miss P is starting to look like her "old-self". With fresh varnish in the helm, and new everything; engines, headliner, wallpaper, wood flooring, curtains and shag carpets through-out, she's looking as good as the day she was first launched, 41 years ago. 



The flooring has allowed the hatches (pictured here before they are covered) to be accessed at any time. Shag throw rugs are being used to cover the main engine hatches, and in the aft cabin, which have been trimmed in the dark oak.


The new headliner has been made in sections of removable panels, there will be thin strips of white wood installed to keep them in position. Like the carpets, wall to wall stretched fabric stapled up made it impossible to gain access anywhere. With the new panels, each section can be dropped down in minutes, exposing wiring runs and allowing thru-deck fittings to be re-sealed, and electronics replaced in the years to come.



G the machinist from Pacific Parts who rebuilt the engines has been busy in the bilges on the weekends doing the cooling side and helping align the engines to the shafts. I joked with him this morning that they are his engines, in Doug's boat. 

He's agreed to be the motor man for Miss P ongoing. He will grow old looking after our gal. The original engines ran for 40 years! With the re-builder being responsible for future servicing and the installation of a fresh water flush kit these should go for 50 more!


The upholstery is back from Jott Industries and they have done a cracker of a job! Adding a small head-roll to the bench and some automotive style piping to the helm seats. The automotive styling we borrowed was not from a car, instead it was taken from the 1968 19' Commander's seats - undoubtedly influenced at the time by Detroit.



Props On! and Off!

Everything was going great, until the resident prop polisher and boatyard's old salt - Don - discovered that they were not a matched set. The prop shop had not polished the barrel of the prop and had used a grinder to clean the blades. Don massages the props with emery paper and doesn't loose a gram of the bronze. Using a grinder to polish a prop he thinks is murder and should be a capital offense. Not to clean the body of the prop - "what kind of prop shop does that!" demands the now cranky Don.

After doing the first, he moved to the second and within minutes he was in a flap - the props don't match! I heard shouted from the stern. When he sanded down the second barrel it was confirmed the two props were a mismatch and somewhere along the line Paramount's two sets of props were mixed-up and one from each pair were on the boat.

If Don didn't give the props the extra care, we would have missed this. In fact we had. They were back on Paramount.

We could have spent the next year trying to figure out what and where the difference was - she might have pulled to one side, she might have vibrated on one side - and we would have checked everything, transmissions, compression and still scratched our heads!



Using the latest $4000. laser tool for aligning the shafts was a solution that ensured true alignment for the very first time for Miss P. 

Dr. Doug discovered the engine stringers were too high and everything after that had been forced - right down the shaft. It was almost impossible to turn the props by hand. Doug took 1/2" off the top off the stringers to allow the engine to sit lower and be adjusted up or down.

With the laser in the shaft-log pointed back, the struts could all be shimmed and aligned dead centre. Tissue paper was stretched over the strut covering the cutlass bearing, the laser was then shot through allowing for an exact centre right the way back through the three struts. It was then shot at the engine and the dead-centre of the coupler was found and the engine mounts moved to facilitate the feeler gauge checking for the correct and perfect alignment.

We should be getting some strong winds in the next few days. I'm hoping to see these props turning in the wind.